Abstract

Due to the fast depletion of fossil fuels and its negative impact on the environment, more attention has been concentrated to find new resources, policies and technologies, which meet the global needs with regard to fuel sustainability and emissions. In this paper, as a step to study the effect of burning low calorific value fuels on gas-turbine performance; a 50 kW slightly pressurized non-premixed tubular combustor along with turbocharger based twin shaft micro gas-turbine was designed and fabricated. A series of tests were conducted to characterize the system using LPG fuel. The tests include the analysis of the temperature profile, pressure and combustor efficiency as well as air fuel ratio and speed of the second turbine. The tests showed a stable operation with acceptable efficiency, air fuel ratio, and temperature gradient for the single and twin shaft turbines.

Details

Title
Experimental Investigation of A Twin Shaft Micro Gas-Turbine System
Author
Shaharin Anwar Sulaiman 1 ; Idris, Ibrahim 1 

 Mechanical Engineering Department, Universiti Teknologi PETRONAS, Bandar Seri Iskandar, 31750 Tronoh, Perak, Malaysia 
Publication year
2013
Publication date
Jun 2013
Publisher
IOP Publishing
ISSN
17551307
e-ISSN
17551315
Source type
Scholarly Journal
Language of publication
English
ProQuest document ID
2534293314
Copyright
© 2013. This work is published under http://creativecommons.org/licenses/by/3.0/ (the “License”). Notwithstanding the ProQuest Terms and Conditions, you may use this content in accordance with the terms of the License.