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© 2024 by the authors. Licensee MDPI, Basel, Switzerland. This article is an open access article distributed under the terms and conditions of the Creative Commons Attribution (CC BY) license (https://creativecommons.org/licenses/by/4.0/). Notwithstanding the ProQuest Terms and Conditions, you may use this content in accordance with the terms of the License.

Abstract

In experiments of aviation motor bearings, when the deep-groove ball bearings are subjected to an overturning moment at high speed, it often happens that the rivet on the cage breaks and the debris invades the raceway, resulting in bearing failure. To address the problem of early failure of deep-groove ball bearing cages and rivets in aviation motors, the causes of early failure were analyzed from the aspect of cage design in this study. The influence of the raceway and cage structure parameters on the dynamic contact characteristics of the rolling element and cage under the action of overturning torque were analyzed, the weak link of the cage was determined, and the cage design parameters were optimized. The results show that with an increase in the cage width and pocket radius, the impact force between the ball and cage first decreases and then increases, and the tilt angle of the cage gradually decreases. A larger channel radius and smaller clearance can slow down the interaction between the cage and the rolling element and make the cage run more smoothly. Increasing the thickness of the cage can ensure that the rivet part of the cage is at a low stress level, and the risk of premature fatigue failure at the rivet part can be reduced by maintaining a small gap–fit relationship between the rivet and rivet holes. The research results indicate that the working condition adaptability of the bearing cage for aviation motors can be improved, and the design method for this type of bearing can be enhanced.

Details

Title
Failure Inducement Factor Analysis and Optimal Design Method of Ball Bearing Cage for Aviation Motor
Author
Cui, Yongcun 1 ; Cai, Linshen 2 ; Wang, Jingjing 3 ; Gao, Xiaoguo 3 

 School of Mechatronics Engineering, Henan University of Science and Technology, Luoyang 471023, China; Changzhou NRB Corporation, Changzhou 213000, China 
 School of Mechatronics Engineering, Henan University of Science and Technology, Luoyang 471023, China 
 Key Laboratory of Power Transmission Technology on Aero Engine, Aero Engine Corporation of China, Shenyang 110015, China 
First page
466
Publication year
2024
Publication date
2024
Publisher
MDPI AG
e-ISSN
20751702
Source type
Scholarly Journal
Language of publication
English
ProQuest document ID
3084973521
Copyright
© 2024 by the authors. Licensee MDPI, Basel, Switzerland. This article is an open access article distributed under the terms and conditions of the Creative Commons Attribution (CC BY) license (https://creativecommons.org/licenses/by/4.0/). Notwithstanding the ProQuest Terms and Conditions, you may use this content in accordance with the terms of the License.